North Sea Well Access Restored Through Intelligent Wireline Intervention Well-Safe Solutions Recovers 11,575 ft of Slickline Lost in a Well After 15 Years Collection of data with minimal pressure loss in flowing wells Contingency barrier option on high-value subsea wells Recovery of magnetic junk in high temperature wells Hard scale removal at multiple obstruction points Retrieval of equipment lost in the well and fast-track production restart High deviation, heavy-duty fishing, North Sea > Recovery of safety valve lockout tool which had parted downhole Retrieval of sub-surface safety valve (SSSV) with damaged fish neck Retrieval of injection valve backed off from 7-in retrievable bridge plug Trial deployment of slickline-set SIM plugs and Peak latch/seal micro coil stinger Data acquisition to monitor pressure buildup in a shut-in well Bespoke activation tool design Evaluation of an e-line deployed tractor, stroker, and slickline toolstring Trial test to remove hard scale from production tubing using mechanical means Cut wire at rope socket to retrieve stuck toolstring Retrieval of injection valve from tubing crossover at 10,400 ft High-deviation fishing at depth in the Middle East Isolation of failed inflow valve at high deviation Location and stabilization of a leak path in the completion string Innovative use of an LWIV to perform first subsea slickline intervention in Nigeria Efficient straddle solution enables repair of production Christmas tree Permanent plug keeps P&A project moving Peak eCutter facilitates faster stuck toolstring recovery in long-reach, highly-deviated well Retrievable sand screen anchoring system eliminates leaks Mechanical scale removal saves USD 250,000 PTTEP gas lift straddle conversion restores oil production for mature well Slickline-deployed plug isolates damage to avoid workover KOC restores oil production to 800 bbl/d using digital-slickline-conveyed straddle system D-Set setting tool and DSL digital slickline cable set large-bore gauge hanger in monobore well Retrievable bridge plug enables proper tubing cut and saves 4 rig days, Congo Remote Intervention Operation Enables Effective Planning of Plug and Abandonment Campaign Shell Removes 900-ft Parted Wireline from North Sea Well Setting a Critical Well Barrier in Tubing with Damaged Nipple Profiles

Recovery of safety valve lockout tool which had parted downhole

 

Technical Challenge:

Recovery of safety valve lockout tool which had parted downhole

Peak Solution:

Fishing package including: high temperature/high strength magnet, releasable overshot, releasable spear

Customer:

Major international oil company, Southern North Sea

Well Type:

Gas producer (66 degree deviation)

Technical Challenge:

The safety valve lockout tool had parted downhole in the safety valve at 534 ft well depth. Video footage established that the ‘bean can’ mechanism (part of the safety valve lockout tool which keeps the flapper permanently in open position) had successfully locked out the downhole safety valve (DHSV). The sub-assembly housing on the bean can had fallen and was expected to be sitting in the 3.688-in nipple at 8155 ft.

Considerations:

It was identified that the actuation dog of the lockout tool might hinder the retrieval of the housing by sitting across the top of the fish, thus preventing retrieval with a spear.

Summary:

In response to the situation, Peak worked in close collaboration with the operator, providing technical support and discussing all the fishing options. Peak provided layout drawings for various overshots and spears, operational procedures, rapid manufacture, and delivery of the fishing tools to Great Yarmouth.

For one contingency, a gauge cutter was heavily modified to act as a sweeping tool for the actuation dog. In the event that it was needed, the gauge cutter would be rotated around the top of the sub assembly by an indexing tool and would push the actuation dog back into the sub assembly. A high temperature/high strength magnet was supplied for retrieval of the actuation dog and a 2.720-in releasable spear for retrieval of the sub assembly.

The high temperature/high strength magnet picked up the actuation dog and the releaseable overshot speared the inner spring mandrel on the first attempt and pulled the fish to surface.

Value to Customer:

The operator was delighted with the successful outcome.

  • Highly effective team work - In response to the situation, Peak collaborated closely with the operator, providing technical support and discussing all the fishing options.
  • Rapid response – Prompt mobilization of fishing tools to Great Yarmouth.
  • Reduced NPT – Expertise and high-performance tools enabled successful fishing on the first attempt.  Production can resume much quicker.

 

Product Code: 115, 204, 230