North Sea Well Access Restored Through Intelligent Wireline Intervention Well-Safe Solutions Recovers 11,575 ft of Slickline Lost in a Well After 15 Years Collection of data with minimal pressure loss in flowing wells Contingency barrier option on high-value subsea wells Recovery of magnetic junk in high temperature wells Hard scale removal at multiple obstruction points Retrieval of equipment lost in the well and fast-track production restart High deviation, heavy-duty fishing, North Sea Recovery of safety valve lockout tool which had parted downhole Retrieval of sub-surface safety valve (SSSV) with damaged fish neck Retrieval of injection valve backed off from 7-in retrievable bridge plug Trial deployment of slickline-set SIM plugs and Peak latch/seal micro coil stinger Data acquisition to monitor pressure buildup in a shut-in well Bespoke activation tool design Evaluation of an e-line deployed tractor, stroker, and slickline toolstring Trial test to remove hard scale from production tubing using mechanical means Cut wire at rope socket to retrieve stuck toolstring Retrieval of injection valve from tubing crossover at 10,400 ft High-deviation fishing at depth in the Middle East Isolation of failed inflow valve at high deviation Location and stabilization of a leak path in the completion string Innovative use of an LWIV to perform first subsea slickline intervention in Nigeria Efficient straddle solution enables repair of production Christmas tree Permanent plug keeps P&A project moving Peak eCutter facilitates faster stuck toolstring recovery in long-reach, highly-deviated well Retrievable sand screen anchoring system eliminates leaks Mechanical scale removal saves USD 250,000 PTTEP gas lift straddle conversion restores oil production for mature well > Slickline-deployed plug isolates damage to avoid workover KOC restores oil production to 800 bbl/d using digital-slickline-conveyed straddle system D-Set setting tool and DSL digital slickline cable set large-bore gauge hanger in monobore well Retrievable bridge plug enables proper tubing cut and saves 4 rig days, Congo Remote Intervention Operation Enables Effective Planning of Plug and Abandonment Campaign Shell Removes 900-ft Parted Wireline from North Sea Well Setting a Critical Well Barrier in Tubing with Damaged Nipple Profiles

Slickline-deployed plug isolates damage to avoid workover

1,300-bbl/d production restored for KOC by installing SIM system retrievable bridge plug with LIVE digital slickline services.

Combining a reliable mechanical plug from Peak Well Systems with LIVE digital slickline services to confirm positioning avoided a workover operation for Kuwait Oil Company (KOC) that would have shut down production on the five-well pad.

The KOC's concerns

KOC noticed a drop in an oil well's production and diagnosed that it was caused by Y-tool circulation. Although the Y-tool had a landing nipple with an installed blanking plug that normally seals during production, there was a leak in the Y-tool.

What KOC tried first

The blanking plug could be retrieved, so KOC replaced it. However, oil production did not recover, indicating that the nipple profile was damaged. Replacing the nipple would require a workover that would shut down the production of all five wells on the pad. And the resulting production loss from the pad would be thousands of barrels of oil.

What was recommended

Schlumberger recommended using LIVE digital slickline services to set a 2 7/8-in SIM sealing integrity management system retrievable bridge plug into the Y-tool bypass tube, sealing it off. The nippleless SIM system plugs can be set anywhere within the tubing, and they can be retrieved and reset at any time if another intervention is conducted. Using LIVE digital slickline services would provide real-time correlation to accurately set the plug. With this solution, KOC would avoid having to conduct a workover operation.

How KOC restored production without a workover

Deploying a SIM system plug on digital slickline enabled efficient installation of the plug in a 2 7/8-in joint below the Y-tool. This restored the well to 1,300-bbl/d production. It also eliminated the expense of workover operations and any production loss from the well and four other wells on the pad during a workover. The operator wrote a commendation letter, seeking to work together again.

 

Product Code: 351